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HomeMy WebLinkAboutFAIRVIEW WEST SIXTH - Filed GC-GENERAL CORRESPONDENCE - 2003-10-20E N G I N E E R I N G L� 1 L-L NELSON, HALEY, PATTERSON AND QUIRK, INC. 2021 CLUBHOUSE DRIVE GREELEY. COLORADO 80631 PHONE 303: 3S2-8077 July 5, 1968 Mr. Roy A Bingma.n City Engineer City of Fort Collins Post Office Box 580 300 West La Porte Ft. Collins, Colorado 80521 Dear Mr. Bingman: Project No. 62 00 018 Re: 24" Storm Drain in Fairview "West", Sixth Filing We have reviewed our design sheets for the 24 inch storm drain in Fairview "West", Sixth Filing with regard to the six inch dip which was constructed in the line at the back of Lots 9 and 10 of Fairview "West", Sixth Filing. As the controlled inlet and outlet conditions and the hydraulic gradient have not been affected, the only result of this small dip is a small increase in the friction factor of the storm drainage line. This increase in the friction factor will have a negligible effect on the carrying capacity of the pipe. At design capacity, the velocity of the water in this pipe is about five feet per second, which will prevent settlement of any solids which might enter the system. Therefore, we feel that this dip will not affect the ability of this 24 inch storm drain pipe to handle the ten year design storm. If you have further questions concerning this matter, please contact us. Very truly yours, NELSON, HALEY, PATTERSON, and QUIRK, INC. Gerald B. McRae, P.E. GBM/lah cc: Mr. William Bartran OFFICES IN GREELEY AND GRAND JUNCTION, COLORADO